Those of you who know a little about using scanners to listen in on radio communications while railfanning know that the industry is changing with CSX is poised to lead the way.

However, this may come at a hefty price to railfans – the adoption of FCC emission designator 4K00F1E, otherwise known as NXDN digital format – something that is not available in any current scanners (not even the high end digital ones).

The NXDN realization hit home early in 2011 here in Lafayette as callsign KEX475, otherwise known as CSX’s license for Shops Yard, was modified to include the new NXDN digital format. This same format is utilized by Christian County for all of it’s public safety communications, and will soon be utilized by Hopkins County public safety. The format is proving very prevalent as a cost alternative to the more universal APCO-25 (like that used by Kentucky State Police and numerous other states).

So is this the end of railroad scanning? No, not yet. The switch is still a ways out, but there’s more than one way to skin the proverbial cat… There is a software application that allows listeners to decode the NXDN format – a similar type setup like myself and Steve Miller utilize to decode the ATCS signals used on CSX’s CTC system. – Chris Dees

 

Chris Dees is searching for information about the locomotives and passenger cars used at the Kaintuck Territory amusement park in Draffenville, Kentucky during the late 1960s and early 1970’s. I’ve seen mention of the ones in the photo links below… just curious.

http://www.steamlocomotive.com/misc/images/showImage.php?image=palmersville1.jpg

http://www.steamlocomotive.com/misc/images/showImage.php?image=palmersville3cz.jpg

http://www.steamlocomotive.com/misc/images/showImage.php?image=palmersville2gm.jpg

I’m also looking for a photo of the NC&StL depot in Benton, Kentucky.  You can contact Chris Dees at chris.dees@trw.com, or phone: (765) 429-1788

Mobile: (765) 586-9138

Fax: (765) 429-1881

Railfan and Railroad magazine is reporting that Jim Boyd has passed away. Jim started with Carstens Publications working on Flying Models and later Railroad Model Craftsman. Jim served as editor of Railfan & Railroad from the magazine’s inception in 1974 until 1998, and continued as Editor Emeritus and author of the popular Camera Bag column until his passing. We’ll pass along details as they become available.

As a side note, I was able to meet Jim at Rochelle, IL during the MILW 261 Grand Excursion a couple years ago. He was a great guy and an ordinary average railfan.  – Chris Dees

Part 1 (Part 2 to follow in January edition)

Submitted by Chris Dees

With the movie “Unstoppable” being released in theaters this Friday, I thought I’d share the official investigation by CSX Transportation regarding the actual incident that the movie is based on.

Synopsis

On May 15, 2001, at approximately 12:35 p.m., DST, an unmanned CSX yard train consisting of one model SD-40-2 locomotive, 22 loaded, and 25 empty cars, 2898 gross trailing tons, departed Stanley Yard, which is located in Walbridge, Ohio. The uncontrolled movement proceeded south for a distance of 66 miles before CSX personnel were able to bring the movement under control. At the time of the incident, the weather was cloudy with light rain. The ambient temperature was 55 degrees Fahrenheit. There was no derailment of equipment or collision. There were no reportable injuries as a result of the incident.

Circumstances Prior to Incident

Yard crew Y11615, consisting of one engineer, one conductor and one brakeman, reported for duty at Stanley Yard, Walbridge, Ohio, at 6:30 am, DST, May 15, 2001. After the normal job briefing with the trainmaster, crew Y11615 performed routine switching assignments until approximately 11:30 am, at which time the crew received new instructions and a second job briefing. A few minutes before 12:30 p.m., the crew entered the north end of track K12, located in the classification yard, with the intent to pull 47 cars out of K12 and then place these cars on departure track D10. Locomotive CSX 8888 was positioned with the short hood headed north. The engineer was seated at the controls on the east side of the locomotive.

The locomotive coupled to the 47 cars on track K12, as instructed and planned. The air hoses between the locomotive and the cars were not connected, as is normal during this kind of switching operation. The air brakes on the cars were therefore inoperative. The brakeman notified the engineer by radio to pull north from K12. After the rear or 47th car passed the brakeman’s location, he walked west to position the switch for the reverse movement to proceed into the assigned track D10.

The movement continued north out of K12 passing the conductor, who was positioned on the ground at the “Camera” switch. The conductor advised the engineer by radio of the number of cars that had passed him and received an acknowledgement from the engineer by radio.

The Incident

With eight cars remaining to pass over the “Camera” switch, the conductor notified the engineer by radio to prepare to stop. The engineer did not respond to his communication. The conductor again notified the engineer when four cars remained to clear the switch, but again there was no response from the engineer. The conductor then ordered the engineer to stop movement, but again there was no response from the engineer and the movement continued.

In his interview, the engineer stated that as he pulled north out of K12, he was notified by radio by the conductor that the trailing point switch for track PB9 off the lead was reversed. The engineer understood that it would be necessary for the movement to be stopped short of the PB9 switch in order to line the switch for movement further along the lead. Neither the conductor nor the brakeman were near the PB9 switch, and the engineer intended to stop his train, dismount from the locomotive, and align the switch to its normal position, if necessary. The speed of the movement up the lead had now reached 11 mph. The engineer observed the reversed switch, but due to the wet rail conditions and the number of cars coupled to his locomotive, he foresaw that he could not bring the equipment to a stop prior to passing through the misaligned switch.

The engineer responded by applying the locomotive’s independent brake to full application. The independent brake applies the brakes on the locomotive but does not apply the brakes on the individual freight cars. In addition, he reduced brake pipe pressure with a 20 psi service application of the automatic brake valve. The automatic brake is pneumatic braking system designed to control the brakes on the entire train. Still certain he would not stop short of the switch the engineer attempted to place the locomotive in dynamic brake mode. The dynamic brake utilizes the locomotive propulsion system to brake the train. Dynamic braking is analogous to down shifting a truck or automobile. Unfortunately, the engineer inadvertently failed to complete the selection process to set up the dynamic brake. Under the mistaken belief that he had properly selected dynamic brake, the engineer moved the throttle into the number 8 position for maximum dynamic braking. The engineer believed that the dynamic brake had been selected and that additional braking would occur. However, since dynamic brake set up had not been established, the placing of the throttle into the number 8 position restored full locomotive power, instead of retarding forward movement of the train.

While the train was still moving at a speed of approximately 8 mph, the engineer dismounted the locomotive and ran ahead to reposition the switch before the train could run through and cause damage to the switch. The engineer was successful in operating the switch just seconds before the train reached it. The engineer than ran along side the locomotive and attempted to reboard. However, the speed of the train had not decreased as the engineer had expected but had increased to approximately 12 mph. Due to poor footing and wet grab handles on the locomotive, the engineer was unable to pull himself up on the locomotives ladder. He dragged along for approximately 80 feet until he released his grip on the hand rails and fell to the ground.

Unable to reboard and stop the movement of his train, the engineer ran to contact a railroad employee, not a member of his crew but in possession of a radio, located at the north end of the yard. This employee immediately notified the yardmaster of the runaway train. The yardmaster promptly notified the Stanley tower block operator and the trainmaster. The Toledo Branch train dispatcher located in Indianapolis was also notified. The movement was now proceeding southward on the Toledo Branch (Great Lakes Division) governed by Traffic Control System (TCS) Rules. The time was approximately 12:35 p.m.

The brakeman observed the train depart the yard but did not initially see the engineer on the ground. The brakeman and another employee used a personal vehicle to pursue the train to the next grade crossing to attempt to board the train. Their immediate concern was for the safety of the engineer, who they feared may have suffered a heart attack while at the controls of the locomotive. At the grade crossing, the two employees were unable to board the train as the speed had increased to approximately 18 mph as it passed the mile post 4. Local authorities and the Ohio State Police were notified of the runaway train at approximately 12:38 p.m.

Attempts to Stop the Runaway

At a siding called Galatea, near mile post 34, at approximately 1:35 p.m., the train dispatcher remotely operated the switch for the train to enter the siding. Previously a portable derail had been placed on the track in an attempt to derail the locomotive and thereby stop the movement. The portable derail was, however, dislodged and thrown from the track by the force of the train passing over it, and the movement of the train was not impeded.

Northbound train Q63615 was directed by the dispatcher into the siding at Dunkirk, Ohio. The crew was instructed to uncouple their single locomotive unit from their train and wait until the runaway passed their location. at approximately 2:05 p.m., the runaway train passed Dunkirk, and the siding was lined for the crew of Q63615 to enter the main track and to pursue the runaway train.

At Kenton, Ohio, near mile post 67, the crew of Q63615 successfully caught the runaway equipment and succeeded in coupling to the rear car, at a speed of 51 mph. The engineer gradually applied the dynamic brake of his locomotive, taking care not to break the train apart. By the time the train passed over Route 31 south of Kenton, the engineer had slowed the speed of the train to approximately 11 mph. Positioned at the crossing was CSX Trainmaster Jon Hosfeld, who was able to run along side the unmanned locomotive and climb aboard. The trainmaster immediately shut down the throttle, and the train quickly came to a stop. The time was 2:30 p.m. and the runaway train had covered 66 miles in just under 2 hours.

An examination of the controls confirmed that the locomotive independent brake had been fully applied, automatic brake valve was in the service zone, and the dynamic brake selector switch was not in the braking mode. All brake shoes had been completely worn to the brake beams. The railroad was prepared to place an additional fully manned locomotive ahead of the runaway south of Kenton, if necessary, to further slow the train. This rather hazardous option was fortunately not required.

(To be continued in January 2011)

CSX announced its timetable for transitioning from wideband (25 KHz) to narrowband (12.5 KHz) railroad radio operation, the American Short Line & Regional Railroad Association reported on September 21, 2010. It is the first Class I railroad to furnish this information for dissemination. The Federal Communications Commission (FCC) has mandated the end of wideband two-way radio transmission for non-military purposes in the U.S. after Jan. 1, 2013. [See Technology, October 2010 TRAINS] The CSX timetable presently calls for the changeover to be completed entirely in 2011.  Submitted by Chris Dees

As Autumn descends on the Midwest, Saturdays are usually set aside for that event known as College Game Day. October 16, 2010, was no exception in Lafayette, Indiana, as the familiar cheer of “Boiler Up – Hammer Down” erupted from Ross-Ade Stadium. However, on this Purdue Homecoming 2010, my friend Doug Buck and I had a different vision of what it means to “Boiler Up and Hammer Down” – one built back in 1907 by the Southern Railway. So we decided to invade “Illini Country” and head west to Monticello, Illinois to ride behind, photograph, and chase newly restored Southern Railway 2-8-0 number 401.

Monticello, Illinois – circa??? With visitors from a nearby Amish community on hand to see Southern 401 come back to life, this shot could easily have been taken 16-October-1910 instead of 100 years later. Photo by Chris Dees
Monticello, Illinois – circa??? With visitors from a nearby Amish community on hand to see Southern 401 come back to life, this shot could easily have been taken 16-October-1910 instead of 100 years later. Photo by Chris Dees
Boiler Up!!! Southern 401 begins the 103rd year of working on the railroad. Here she is crossing Camp Creek en route to the town of Monticello, IL on 16-Oct-2010. Photo by Chris Dees
Boiler Up!!! Southern 401 begins the 103rd year of working on the railroad. Here she is crossing Camp Creek en route to the town of Monticello, IL on 16-Oct-2010. Photo by Chris Dees
Hammer Down!!! Southern 401 stretches her legs in the early morning prior to running excursions for the Monticello Railway Museum. Here she switches out a Wabash boxcar in order to assemble the day’s passenger consist. Photo by Chris Dees
Hammer Down!!! Southern 401 stretches her legs in the early morning prior to running excursions for the Monticello Railway Museum. Here she switches out a Wabash boxcar in order to assemble the day’s passenger consist. Photo by Chris Dees

Ron Stubblefield – I first met Ron Stubblefield in Paducah, Kentucky, during my senior year at Murray State University. Ron had recently joined the Paducah Model Railroad Club and his HO-scale module had a lot of circus-related models: a carousel, a Ferris wheel, and even a Z-scale park train. In the coming months, Ron and I became good friends, culminating in Ron assisting me in getting my first job at Siemens in Ron’s hometown of Marion (KY). 1993 began with Ron and I traveling every Thursday night to Don Clayton’s house in Madisonville and the monthly NRHS meetings. Without Ron, I would not have had a chance to start my career the way I did, and I would not have met many other dear friends – the fellow members of the Western Kentucky Chapter of NRHS. I am forever indebted to Ron and his wife Kay.

Those weekly trips were more (than) just a ride to see trains. They were a small journey on the  Ron-sized path of life. Sure, we saw the P&L Railway take over the Tradewater Railway through Marion, had CSX serenade us during dinner at Burger King in Madisonville, and chased multiple trains in that little Jeep across southern Illinois and Southeast Missouri – including the 1996 Olympic Torch train on Union Pacific. But Ron demonstrated what it was to be a real man – a kind of big brother (and I say that respectfully in terms of his physical size and the size of his heart). I would also not have been able to railfan many local hotspots had I not met Ron – those memories of racing down gravel roads and doing power slides in rural southeast Missouri in pursuit of UP and SP are and will continue to be cherished in the coming years. Ron also taught me a lot about railfan photography and was an incredible teacher of geology. Many of his photos graced multiple issues of our newsletters. And Ron’s knowledge of minerals and his involvement with the Clements Mineral Museum gave me a different view of “those rocks”.

In closing, I will miss my brother Ron. He was a good friend, a great mentor, and the best Christian brother a man could have. But I know, as my pastor Steve Viars would say: “this man knew that he knew that he knew he was on his way to Heaven.” I am sure Ron is enjoying railfanning in Heaven.

Run Eight Ron!!!

Chris (Dees)

Murrel Hogue was a fellow NRHS member, mileage collector, traveling companion with several Madisonville chapter members, and former Amtrak agent at Texarkana, TX. Many of his fellow mileage collectors would purchase Amtrak tickets through the Texarkana agency in order to support and keep the depot open.

Murrel’s many friends in railroading have discussed options for some permanent recognition of Murrel’s years of service and enthusiastic support for rail passenger service.

A bronze plaque is being prepared designating the Texarkana waiting room as the “Murrel Edward Hogue, Jr. Memorial Waiting Room.”  A ceremony is planned to fomalize this designation, with a tentative date of August 28, 2010 in Texarkana.  Once this date is finalized, additional details will be announced. It is hopeful that many of Murrel’s friends might be able to attend.

Contributions toward the cost of this memorial plaque may be sent to:
Griff Hubbard
1270 Brandywine Drive
Longview, TX  75601

With Best Regards,
Chris Dees

burgerEveryone knows that a day of railfanning can build up a hearty appetite. I remember riding with Rex Easterly, Ron Stubblefield, and Keith Kittinger down to Chattanooga several years ago for a chapter trip to TVRM. Somehow along the way we picked up a dozen Dunkin donuts, a large Pizza Hut Super Supreme Pan Pizza, and a family box of Hardee’s fried chicken.  It’s good to know that the legacy of railfanning and good food continues to this day. With both RJ Corman and Buffalo & Pittsburgh crews pulling heavy freights in the Clearfield, PA area, Denny’s Beer Barrel Pub is a great place to hang out after a day of railfanning in the Allegheny Mountain region of northwest Pennsylvania. The 100-pounder costs only $380, but is free of charge if you can finish by yourself in 6 hours. As of yet, many of tried, and all have failed. However, their Wall of Fame includes one lady that woofed down the 3-pound version in only 20 minutes!!!  – Chris Dees

Submitted by Chris Dees

Do Not Hump – Norfolk Southern announced Wednesday, July 15, 2009, that they will close part of the operations at its Sheffield rail yard, a move that involves cutting 84 jobs. Robin Chapman, a spokesman for Norfolk Southern in Atlanta, said about 130 people work at the yard.

The rest of the local rail yard will remain open, company officials said. Chapman said 57 layoffs are train and engine positions, and 27 are mechanical employees. “The humping operations will be going to Chattanooga or Birmingham,” he said. “There will be some switching operations going to Decatur.”

Chapman said the nation’s economic climate forced the move. “The reason we’re idling humping operations is because of the traffic conditions,” he said. “In this economy, traffic is way down and we can’t support humping operations at Sheffield.” The rail yard is just east of the overpass on Wilson Dam Road, but is referred to as the Sheffield yard by company officials.

Those being laid off will be sent home immediately when the announcement is made Wednesday, but receive pay for 60 days, under a labor agreement, Chapman said. Chapman said employees work on a seniority basis, so those affected by layoffs can displace employees with less seniority in other cities within the railroad’s seniority district, which includes company operations in Alabama and Tennessee.

“The jobs could come back, theoretically, if we resumed humping operations at Sheffield,” Chapman said. “But whether specific employees could come back, that depends where they go and what they do from this point. The ones laid off are on furlough status and would be recalled by seniority.” He said trains will continue to travel through the area and local trains that serve area industries will continue to do so. “Traffic stays the same, it’s just they wouldn’t be humped in Sheffield.”


This is the information that is now available on the regular trips over the Madison Railroad for their Bicentennial event.  I have not heard back about request for a special mileage trip.

Final Plans as of 5/1 Tickets Go On Sale At 9 am, June 1, Heritage Center, 615 W. First Street, Madison.

Here’s the information you need to get your tickets for the Bicentennial Express Train Ride that is sponsored by the Jefferson County Historical Society, Madison Railroad, and the Madison Bicentennial. Tickets are $20 each; there is a limit of 10 per person.  350 Tickets

Cash or checks, NO Credit Cards, NO Debit Cards. Children if small enough to ride in your lap, FREE, BUT IF they take a seat it is $20.

Train leaves the Venture Out Business Center RR MP 41?)  on Wilson Avenue, goes to Middle Fork Bridge (RR MP 35.25).  (about 6 miles one way, 12 total)

NO restrooms on board, only at loading site (Venture Business Center). Saturday Oct 17, Departures 10 am, 1pm 3:30 pm. Sunday Oct 18, Departures 12 Noon, 2:30pm. Ph 812.265.2335

City of New Orleans to Orlando?

Forwarded from the Memphis Railfans Yahoo Group. Posted by: “Tom Parker” tscottparker@gmail.com ts_parker Date: Thu Apr 30, 2009 1:12 pm ((PDT))

I received the following from Amtrak today:
NATIONAL RAILROAD PASSENGER CORPORATION 1001 Loyola Avenue, New Orleans, LA 70113

As you may be aware, the Passenger Rail Investment and Improvement Act of2008 (PRIIA, Public Law 110-432) requires Amtrak to deliver to Congress a plan for restoring rail passenger service between New Orleans, Louisiana, and Sanford, Florida:

Division B, Section 226: Within 9 months after the date of enactment of this Act, Amtrak shall transmit to the Committee on Transportation and Infrastructure of the House of Representatives and the Committee on Commerce, Science, and Transportation of the Senate a plan for restoring passenger rail service between New Orleans, Louisiana, and Sanford, Florida. The plan shall include a projected time line for restoring such service, the costs associated with restoring such service, and any proposals for legislation necessary to support such restoration of service. In developing the plan, Amtrak shall consult with representatives from the States of Louisiana, Alabama, Mississippi, and Florida, railroad carriers whose tracks may be used for such service, rail passengers, rail labor, and other entities as appropriate.

Accordingly, Amtrak assembled a team to meet this objective. The group examined multiple service and schedule scenarios and has narrowed the list to three that were the most operationally feasible. These include the former Sunset Limited as it operated prior to Hurricane Katrina; operating the City of New Orleans through from Chicago, via New Orleans, on a daily basis to Orlando; and a stand-alone service operating daily on an overnight schedule between New Orleans and Orlando with connections in New Orleans and Jacksonville.

Amtrak intends to submit a report to Congress based on these three scenarios and the costs associated with them on or before the July 16,2009, deadline. I hope this information is helpful in your evaluation of the possibilities for restoring service east of New Orleans.

Sincerely,

Thomas L. Stennis III Director,

Government Affairs-South

The Royal Deeside Railway
The Royal Deeside Railway

A few years ago, my cousin Martha Dees (known to the family as Marty) researched the family tree back some 14 generations to our 12th great-grandfather who left the ancestral home in Scotland to come to the new world. The region just southwest of Aberbeen, is known as Deeside and is along the River Dee – hence the basis for our last name. The area is rich in history, is the site of the Royal Bayoral Castle, and includes an interesting and very active historical railway group – the Royal Deeside Railway.

The story of the Royal Deeside Railway dates back to 1845, when the prospectus for the Deeside Railway was issued. This was to be a single-line railway from Aberdeen to the town of Banchory, following the north side of the Dee river throughout. The scheme was so well received that it was decided to extend the line from Banchory through Kincardine O’Neill to Aboyne, just over 29 miles from Aberdeen.

Authorized on 16 July 1846, the Deeside Railway was delayed by the construction of the Aberdeen Railway from Forfar, and the scheme was re-authorized on 28 May 1852, although the Aboyne extension was postponed to a later date. The Deeside Railway opened to traffic on 8th September 1853. Eventually the line was extended to Aboyne in 1857 and reached Ballater on 17 October 1866.

Amalgamated with the Great North of Scotland Railway by 1876, the Deeside Railway was one of the region’s most scenic railway lines and for many years was travelled by members of the Royal Family en route to Balmoral Castle. Indeed, Queen Victoria’s desire for privacy at Balmoral Castle was the reason why the Deeside Railway never continued as planned to Braemar at the top of the Dee Valley.

Although the Deeside Railway was one of the most scenic and picturesque lines in the Aberdeenshire area, the line was mentioned in the Beeching Report of 1963 as a loss-making railway, closing to passengers on 28th February 1966. Goods traffic to the Culter Paper Mills kept the line open for freight until 30 December 1966, when Class B1 Steam Locomotive No. 61180 became the last steam train to run on the Deeside Railway. Arnott Young Ltd. were given the task of dismantling the line and by 1972 the tracks of the Deeside Railway had been lifted.

From 1972 the route of the railway slowly began to be reclaimed by nature, although the former trackbed, station buildings and bridges remained clearly visible to the public. Over time portions of the route were converted for other uses, the trackbed between Holburn Street & Culter being surfaced as a popular cycle & walking route. Other changes were more dramatic, such as the removal of the Holburn Street Bridge in 1981, the demolition of the station site at Banchory for construction of housing, and the complete dismantling of the Blarnacrag (or Beltie) Viaduct between Torphins & Lumphanan. However the majority of the route is still easily visible some 40 years after the railway was closed.

The Royal Deeside Railway Preservation Society was formed in 1996 by local railway enthusiasts, initially concentrating its efforts at the Aberdeen end of the line, where part of the former Aberdeen Ferryhill Engine Shed was considered for use as a workshop & museum, along with heritage railway services on the section of former Deeside Railway trackbed adjacent to the shed site. Discussions on the acquisition of the shed site are continuing with Network Rail & Aberdeen City Council.

the Royal Deeside Railway
the Royal Deeside Railway

In August 2000 the society submitted plans to the local council for a reinstated railway operation between Banchory and Milton of Crathes, on the former Deeside Railway Line. Recent European Legislation required an “Environmental Impact Assessment” to be carried out, which was submitted in 2002. Approval for the majority of the scheme was received on 10th June 2003, work starting at the Milton end shortly thereafter.

The Society now has a number of items of rolling stock under restoration, including the unique “Battery Railcar” which ran on the line in the 1950s, and a historic collection of vintage Victorian coaches which are under restoration for use on the line. Regular summer execursions were started in 2008 and already the railway is beginning to come back to life.

Website address: http://www.deeside-railway.co.uk/index.php